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Click On Image To Enlarge80s Major RF-4B Phantom Mishaps
By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
The RF-4B Phantom, the Marine Corps’ answer to the question, “How much camera gear can you cram into a jet before it starts flying like a drunken daulphin?” She was the recce pig you got stuck with when you lost a bet, and her idea of self-defense was hoping the enemy died laughing. Flying solo, low, and fast, because apparently, we liked our odds against both gravity and common sense, the RF-4B’s mishap record reads like a daredevil’s medical chart. Nose-High Trap? That snout was so long, you needed a periscope to see the deck. Get behind the power curve, and you’d be swimming with the fishes before the J79s even woke up. Hydraulics? More like hydraulic roulette. Lose the utility system, and you’d better hope the barrier crew had their Wheaties, because you were coming in hot with the gear half down and the flaps somewhere in the next zip code. And don’t get me started on the photoflash racks, one spark in there and you’d light up the night sky like a Fourth of July gone horribly wrong. Welcome to recce, devil dog. Try not to set yourself on fire.


RF-4B Phantom Mishaps
1980 - 1990
RF-4B Texas Crash, PDF
Aircraft RF01 #151975 (Pilot) Lt. Col. Burton P Sperry III
(RSO) Capt. Michael S Fagen Eject.

25 May, 1980-The aircrew made safe ejections. Capt. Fagan ejected through the rear canopy; the oxygen supply then failed to activate due to a flaw in the design of the activator switch; then the drogue slug struck the NES-8B parachute canopy, tearing a hole in one panel. He suffered a minor concussion and separated shoulder--he was transported from the scene by civilian ambulance. Lt.Col Sperry was located by a civilian policeman on routine patrol; he then apparently returned to NAS Dallas aboard t he Marine Reserve MAG-41 Sikorsky CH-53 Sea Stallion helicopter dispatched to the scene....Read More.

RF-4B Nevada Crash
Aircraft RF24 #153101
Pilot Lt. Pete keenan
RSO Lt. Bill Lauerman

By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
22 May, 1981-This is my version of the events of that accident. At that time, 1981, it was common practice in the squadron to launch aircraft on Fridays for weekend hops. I was in charge of aircraft RF24 on 22 May, that Friday morning. For some reason, I had my pocket camera with me and took this photo just before Lt Lauerman climbed into the back seat. I had already helped strap Lt Keenan in the front seat. This is the time anyone in the squadron would ever see them again. It was a normal launch, and I taxied them out, saluted Lt Keenan, and he returned the salute, and off they went....Read More.

RF-4B Iwakuni Crash
Aircraft #157342
(Pilot) Capt. Chuck Overstress Strong
(RSO) Capt. Terry T-Bird Sweeney
By Capt. Terry T-Bird Sweeney / Updated Dec. 2025
11 Jan.1983-I was flying with Capt. Chuck "overstress" Strong on January 11, 1983 in Iwakuni. We were on short final, when we had a duel engine flame out. Overstress yelled. "Hang on T-Bird." The next thing I knew I was flying Martin Baker. He had "punched us out." The aircraft was # 157342. However, the plane ended up landing by itself. In fact it only had class "B" damage. It is the only jet in the history of military aviation (Navy, Marine, Air Force) that anyone ever ejected out of, that flew again.


RF-4B USS Midway Crash
Aircraft RF25 #153109
(Pilot) Capt. Mike Healey
(RSO) Maj. John Yencha
January 1984
Maj. John Yencha (RSO) and Capt. Mike Healey (pilot in command) of VMFP-3, Det. Alpha, were on a routine reconnaissance mission during midday cyclic operations in the Indian Ocean when their RF-4B Phantom II experienced a utility hydraulic failure. Healey immediately turned the aircraft back toward the USS Midway while Yencha contacted strike and notified the ship of their situation. A short discussion aboard the Midway ensued and it was decided that a barricade landing would be attempted as per NATOPS. Air operations notified the aircrew of the decision and went over the plan with them. Meanwhile, below, on the deck of the Midway, all three of the arresting cables were pulled and the barricade was rigged. Flying at 5,000 feet downwind, Healey blew the flaps down and turned inbound for a five-mile straight-in approach. Paddles took control from one mile out. As the RF-4B crossed the round-down, the LSO gave the command "CUT!," and the result was a picture-perfect barricade engagement. Video Top Of Page

RF-4B Philippines Crash
Aircraft RF25 #153109
(Pilot) Capt. Huey D. Moser Jr.
(RSO) 1Lt. Andrew C. Auer
27 Oct. , 1987

As Shark 71 entered the photoflash run the left side ejector raks fired normally; when the right side ejector racks began to fire seven cartridges fired normally; the eighth did not fire, remaining in the rack; the ninth cartridge fired normally; the tenth cartridge failed to eject from the rack. The 'fired but not ejected' cartridge exploded, causing a small pinhole leak in the Power ControlII (PCII) hydraulic system. The leak atomized and caught fire which in turn burned through the aileron rudder interconnect system wire bundle. Whenthe fire burned into/through the wire bundle an uncommand 5-10 degree instantaneous rudder input caught the aircrew by suprise. The aircrew immediately ejected, losing their helmets, oxygen masks and velcro covers from their SV-2 vests. After the aircrew ejected the aircraft continued to pitch up to almost 90 degrees and decelerate to zero airspeed at which time the aircraft fell away on the left wing to almost 90 degree nose down until impact with the ground. The crash occured 29 mi generally north from NAS Cubi Point. The Range Safety Monitor initiated the SAR recovery efforts immediately--the USAF SAR helicopter was on the site in under ten minutes. The aircrew was helolifted to Clark AB where they underwent the medical checks. Some 98% of the wreckage was recovered with the aft fuselage section transfered to the NARF depot for investigation of the photoflash malfunction.
Watch The Video


RF-4B California Crash
Aircraft RF32 #157347
(Pilot) Lt. Jon A. Barber
(RSO) Capt. Tim P. Hewitt
09 May, 1990
By Rich Rentrop / Updated Dec. 2025
Was lost at sea off the coast of San Clemente Island. The aircrew made a successful ejection. The mission was a Day FAM Flight filed for IFR/VFR, VMC over the W-291 range. The aircrew was engaged in aerobatics when the aircraft departed controlled flight. The aircraft crashed due to a stall spin.


Click On Image To Enlarge FlashBack Trivia
Naval Air Facility
El Centro, CA By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
RF-4B 151979 that took a barracade trap aboard the USS Midway Jan. 1984 when it's nose landing gear failed to deploy. It was taken out of service and strangly converted to look like a F-4J Blue Angel Phantom and placed on display in the Blue Angel Park at the Naval Air Facility, El Centro, California.


Alright, you glorious Rat Phixers and Phlyers, if we ever survived a TAD, a Det, or a BOHICA, who haven't, and you didn’t think I was the biggest gaff off in the squadron. Got a sea story, or some grainy photos your ex didn’t set on fire, and they’re only slightly illegal? Send ‘em by email, snail mail, or safety wire it to a carrier pigeon. I collect ‘em all, just nothing that would incriminate me.
80svmfp3@gmail.com


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