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80s Major RF-4B Phantom Mishaps
By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
The RF-4B Phantom, the Marine Corps’ answer
to the question, “How much camera gear can
you cram into a jet before it starts flying
like a drunken daulphin?” She was the recce
pig you got stuck with when you lost a bet,
and her idea of self-defense was hoping the
enemy died laughing. Flying solo, low, and
fast, because apparently, we liked our odds
against both gravity and common sense, the
RF-4B’s mishap record reads like a daredevil’s
medical chart. Nose-High Trap? That snout
was so long, you needed a periscope to see
the deck. Get behind the power curve, and
you’d be swimming with the fishes before
the J79s even woke up. Hydraulics? More like
hydraulic roulette. Lose the utility system,
and you’d better hope the barrier crew had
their Wheaties, because you were coming in
hot with the gear half down and the flaps
somewhere in the next zip code. And don’t
get me started on the photoflash racks, one
spark in there and you’d light up the night
sky like a Fourth of July gone horribly wrong.
Welcome to recce, devil dog. Try not to set
yourself on fire.

RF-4B Phantom Mishaps
1980 - 1990
RF-4B Texas Crash, PDF
Aircraft RF01 #151975
(Pilot) Lt. Col. Burton P Sperry
III
(RSO) Capt. Michael S Fagen Eject.
25 May, 1980-The aircrew made safe ejections.
Capt. Fagan ejected through
the rear canopy; the oxygen supply
then failed to activate due
to a flaw in the design of the
activator switch; then the drogue
slug struck the NES-8B parachute
canopy, tearing a hole in one
panel.
He suffered a minor concussion
and separated shoulder--he was
transported
from the scene by civilian ambulance.
Lt.Col Sperry was located by
a civilian
policeman on routine patrol;
he then apparently returned to
NAS Dallas
aboard t
he Marine Reserve MAG-41 Sikorsky
CH-53 Sea Stallion helicopter
dispatched
to the scene....Read More.
RF-4B Nevada Crash
Aircraft RF24 #153101
Pilot Lt. Pete keenan
RSO Lt. Bill Lauerman
By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
22 May, 1981-This is my version of the events
of that accident. At that time, 1981, it
was common practice in the squadron to launch
aircraft on Fridays for weekend hops. I was
in charge of aircraft RF24 on 22 May, that
Friday morning. For some reason, I had my
pocket camera with me and took this photo
just before Lt Lauerman climbed into the
back seat. I had already helped strap Lt
Keenan in the front seat. This is the time
anyone in the squadron would ever see them
again. It was a normal launch, and I taxied
them out, saluted Lt Keenan, and he returned
the salute, and off they went....Read
More.
RF-4B Iwakuni Crash
Aircraft #157342
(Pilot) Capt. Chuck Overstress
Strong
(RSO) Capt. Terry T-Bird Sweeney
By Capt. Terry T-Bird Sweeney / Updated Dec. 2025
11 Jan.1983-I was flying with Capt. Chuck
"overstress" Strong on January
11, 1983 in Iwakuni. We were on short final,
when we had a duel engine flame out. Overstress
yelled. "Hang on T-Bird." The next
thing I knew I was flying Martin Baker. He
had "punched us out." The aircraft
was # 157342. However, the plane ended up
landing by itself. In fact it only had class
"B" damage. It is the only jet
in the history of military aviation (Navy,
Marine, Air Force) that anyone ever ejected
out of, that flew again.
RF-4B USS Midway Crash
Aircraft RF25 #153109
(Pilot) Capt. Mike Healey
(RSO) Maj. John Yencha
January 1984
Maj. John Yencha (RSO) and Capt. Mike Healey
(pilot in command) of VMFP-3, Det. Alpha,
were on a routine reconnaissance mission
during midday cyclic operations in the Indian
Ocean when their RF-4B Phantom II experienced
a utility hydraulic failure. Healey immediately
turned the aircraft back toward the USS Midway
while Yencha contacted strike and notified
the ship of their situation. A short discussion
aboard the Midway ensued and it was decided
that a barricade landing would be attempted
as per NATOPS. Air operations notified the
aircrew of the decision and went over the
plan with them. Meanwhile, below, on the
deck of the Midway, all three of the arresting
cables were pulled and the barricade was
rigged. Flying at 5,000 feet downwind, Healey
blew the flaps down and turned inbound for
a five-mile straight-in approach. Paddles
took control from one mile out. As the RF-4B
crossed the round-down, the LSO gave the
command "CUT!," and the result
was a picture-perfect barricade engagement.
Video Top Of Page
RF-4B Philippines Crash
Aircraft RF25 #153109
(Pilot) Capt. Huey D. Moser Jr.
(RSO) 1Lt. Andrew C. Auer
27 Oct. , 1987
As Shark 71 entered the photoflash
run the left side ejector raks
fired normally;
when the right side ejector racks
began to fire seven cartridges
fired normally;
the eighth did not fire, remaining
in the rack; the ninth cartridge
fired normally;
the tenth cartridge failed to
eject from the rack. The 'fired
but not ejected'
cartridge exploded, causing a
small pinhole leak in the Power
ControlII
(PCII)
hydraulic system. The leak atomized
and caught fire which in turn
burned through
the aileron rudder interconnect
system wire bundle. Whenthe fire
burned into/through
the wire bundle an uncommand
5-10 degree instantaneous rudder
input caught
the aircrew
by suprise. The aircrew immediately
ejected, losing their helmets,
oxygen masks
and
velcro covers from their SV-2
vests. After the aircrew ejected
the aircraft
continued
to pitch up to almost 90 degrees
and decelerate to zero airspeed
at which
time the aircraft
fell away on the left wing to
almost 90 degree nose down until
impact with
the ground.
The crash occured 29 mi generally
north from NAS Cubi Point. The
Range Safety
Monitor
initiated the SAR recovery efforts
immediately--the USAF SAR helicopter
was
on the site
in under ten minutes. The aircrew
was helolifted to Clark AB where
they underwent
the medical
checks. Some 98% of the wreckage
was recovered with the aft fuselage
section
transfered to the
NARF depot for investigation
of the photoflash malfunction.
Watch The Video
RF-4B California Crash
Aircraft RF32 #157347
(Pilot) Lt. Jon A. Barber
(RSO) Capt. Tim P. Hewitt
09 May, 1990
By Rich Rentrop / Updated Dec. 2025
Was lost at sea off the coast
of San Clemente Island. The aircrew
made a successful ejection. The
mission was a Day FAM Flight
filed
for IFR/VFR, VMC over the W-291
range. The aircrew was engaged
in
aerobatics when the aircraft
departed controlled flight.
The aircraft crashed due to a
stall spin.
FlashBack Trivia
Naval Air Facility
El Centro, CA
By Marc "Devil Dog Of The Web" Iseli / Updated Dec. 2025
RF-4B 151979 that took a barracade
trap aboard
the USS Midway Jan. 1984 when
it's nose landing
gear failed to deploy. It was
taken out of
service and strangly converted
to look like
a F-4J Blue Angel Phantom and
placed on display
in the Blue Angel Park at the
Naval Air Facility,
El Centro, California.
Alright, you glorious Rat Phixers and Phlyers,
if we ever survived a TAD, a Det, or a BOHICA,
who haven't, and you didn’t think I was the
biggest gaff off in the squadron. Got a sea
story, or some grainy photos your ex didn’t
set on fire, and they’re only slightly illegal?
Send ‘em by email, snail mail, or safety
wire it to a carrier pigeon. I collect ‘em
all, just nothing that would incriminate
me.
80svmfp3@gmail.com

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